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The
Monterey Bay Aquarium (Monterey, Calif.) is home to more than
550 species of plants and animals that live, eat, and breathe
thanks to the ocean water pumped from the bay straight into
more than 100 tanks and exhibits that these creatures call home.
Each day, the aquarium pumps
nearly 3 million gallons of seawater through the facility
to simulate the natural ocean environment. At night, incoming
seawater is unfiltered, bringing in plankton, seaweed spores,
larvae, and other miniscule food sources for fish and plants.
During the day, however, the raw seawater must be filtered
to keep the tanks and water as clear as possible for visitors.
Fishing
for a solution
When the aquarium opened in 1984, most life-support systems
and filtration were handled manually. This system was vulnerable
to variances in staffing schedules and human error, and required
staff to be on-site 24 hours a day to make sure that all aquarium
processes ran smoothly. As the aquarium expanded (opening
its Outer Bay Wing in 1996 nearly doubled the exhibit space),
one realization became clear—the aquarium would have to dramatically
increase on-site staff or use advanced automation technologies
to maintain required operational efficiencies.
The Monterey Bay Aquarium had
one primary goal when it evaluated automation companies—the
new system had to be a seamless single-vendor solution from
processor to operator interface and beyond. This would ensure
that all components of the system worked together and would
be scalable for future enhancements. The system also had to
be built on open technologies for the same reasons. Because
the aquarium systems run 24 hours a day, its operators had
to be able to learn, operate, and maintain every component
without any outside technical support, in case problems occurred
outside normal technical support hours.
"Increasing staff was not the
best option for us; we wanted to shift our efforts from routine
operations to preventive maintenance," says Mike Brigham,
systems control engineer for the aquarium. "Automation would
give us more consistent controls and allow operators to spend
more time optimizing processes, rather than just keep them
up and running."
After evaluating several vendors,
the aquarium chose Rockwell
Automation (Milwaukee, Wis.) and system integrator Pipeline
Systems Inc. (PSI). PSI mapped out a new control system,
eventually tying in nearly 30 Allen-Bradley SLC 500 programmable
controllers to run various components of life support, as
well as the aquarium's heating/ventilation/air conditioning
(HVAC) system.
A
whale of an idea
The control system now provides automation, monitoring, and
alarming for all principal parameters of the life support
system, including temperature, flow, pressure, dissolved oxygen,
pH, ozone injection, and ORP. It also controls repetitive
tasks like backwashing sand filters for filtration, boiler
and chiller loop control for temperature control, ozone generator
control, and oxygen injection control to maintain oxygen levels
in the water.
In addition, the SLC controllers
handle exhibit lighting for visitors on the other side of
the aquarium glass. The controls automatically turn on and
off all the exhibit, public space, emergency, and housekeeping
lighting to conserve power and create task lighting that enhances
each exhibit area.
Two control rooms at the aquarium
serve as dual headquarters for operators, with operator interface
stations running Rockwell Software RSView32 human-machine
interface (HMI) software on the Microsoft Windows NT operating
system. RSView32 allows control operators to monitor every
control parameter from either control room location, and provides
trending information and alarm notification. Mr. Brigham is
upgrading the system from Rockwell Software's ControlView
HMI DOS to take advantage of new modules available for RSView32.
He recently added the new RSView32 Messenger module, a remote
notification add-on that seamlessly integrates into RSView32
through the HMI's Add-On Architecture environment.
Quick notification of alarms
is critical at the aquarium. If a system failure occurs and
is not corrected quickly, millions of dollars in plant and
animal life could be at risk. Before using Messenger, operators
were required to stay on site so alarms could be heard and
corrected within minutes.
"The Messenger module automatically
alerts the operator on duty by sending an alarm directly to
a pager," Mr. Brigham said. "The ability to receive alarms
off site has allowed us to cut down from 24-hour on-site support
to 18 hours. Now during off-duty hours, the operator can be
paged at home and access the control system remotely through
third-party software."
For some alarms, like a utility
power failure, operators must still return to the aquarium,
but most alarms can now be handled through the remote interface
with Messenger. In addition to alarms, Messenger can provide
status information on processes for off-duty operation or
supervision of multiple processes.
Schools
of information
A main data server logs information collected from control
devices across the aquarium via a local area network and stores
it for use by other departments. Internal departments such
as Applied Research and Animal Husbandry archive certain information
for biological diagnostics research, and outside educational
institutions use some of this information for research.
This continuous data acquisition
allows the biological department to automatically track critical
information that was previously tracked manually. Also, the
biological department can now consistently determine feeding
patterns, temperature variations, and water quality changes
to help maintain the best aquarium environment possible.
The control system has permitted
the aquarium to easily install and maintain total redundancy
on a number of critical life support systems. This ensures
that normal operation can continue on these systems, even
in the event of a primary systems failure with no operator
backup. Remote alarming can notify an operator of any failure,
but having redundant systems eliminates the possibility of
complete failure, in case operators cannot get to the aquarium
quickly.
"The automation systems now in
place have allowed the aquarium to increase in size, increase
efficiencies, respond more effectively to alarms, and collect
information in a more consistent manner," Mr. Brigham says.
"Since inception, the aquarium has grown nearly 300%. However,
with automation technologies, our control systems staff has
only increased about 20%. Now, the time we spend with the
system is focused on perfecting it, rather than operating
it."
Mr. Brigham and his staff continue
to upgrade the current control system. Every few years the
aquarium adds new exhibits or renovates existing ones, which
requires modifications in the control system. As older exhibits
are renovated, older SLCs are swapped out for new, software
is updated, and new sensors are added. Entire exhibits can
be added or moved, which requires flexibility from the systems
and Mr. Brigham's staff, who must keep up with all the changes.
In addition to regular modifications, he also plans to install
new controllers in remote off-site buildings that have previously
been stand-alone systems, tying even more areas to the system.
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written by: Gary
A. Mintchell
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